Ampeg V4B Bass Amp Refurbishment

This wonderful old Selmer-era Ampeg bass head was pulled out of its retirement in the closet and put back into service.  But it had a few issues to address, so that it could reliably pump out the tones that is the Ampeg Experience.

 

01V4B the patientThis unit appears to be absolutely factory stock.  The Houston humidity has had an effect on the aluminum faceplate.

02V4V rear pnl1Taking a tour of the rear panel, we see a bracket upon which the line cord may be wrapped.

03V4B rear pnl2The convenience outlet is a three-prong unit, which is nice.  The hum balance control adjusts the bias current in the output tubes to be the same.

04V4B rear pnl3Magnavox owned both Selmer and Ampeg for a while, if I recall correctly.  Note the tube layout information.

05V4B rear pnl4Here is the other bracket for the cord, and the output jacks and impedance switching.

06V4B cordDude, are you still smoking?

07V4B internals1This is a nice intersection between hand wiring and the use of an etched circuit board.

08V4B internals2This cap and the bleeder resistors are slated for replacement.

09V4B cap1Yes, you can still get multi-section capacitors if you shop diligently.

10V4B cap2The prongs of the new capacitor need to fit in the slots in the chassis.

11V4B cap3There is plenty of height inside the chassis, but it doesn’t hurt to document what we have.

12V4B cap4Likewise, we’re documenting what we have.

13V4B cap1Here is the new multi-sectioned filter capacitor and the hole where it goes in the background.

14V4B cap2The outer can of all of the capacitors is isolated from the chassis, so these green fiberglass spacers are used under the capacitor.

15V4B cap3I think we’re done here!

16V4B cap4The new cap looks nice on the top of the chassis.

17V4B cap3The axial filter capacitor will be replaced with this part.  I am forming the leads to appear in a manner similar to the original part, seen above.  A little Teflon insulating tubing helps keep the electricity under control.

18V4B cap4Wires will be attached to the terminals, so the leads are formed into a loop to accept the wires.

19V4B cap5The wire bending is done with a hand-tool called “chain nose pliers.”

20V4B cap6The original part has a mounting ring around it.  We will need to recycle this mounting scheme to maintain originality.

21V4B cap7The ring is off!  I was a little concerned that I would mess it up, but a little heat was all it took.

22V4B cap8Here is the original mounting ring applied to the new capacitor.

23V4B cap9The ring can slide around just a little bit to give us a nice-looking mounting solution.

24V4B cap10And here we are, all wired up and ready to go back to work.

25V4B good capsThese guys have been replaced recently, and they check out as new.  So, they will remain in service.

26V4B controlsSome of the front panel slide switches were dirty, so some cleaner and lubricant were sprayed into them.

27V4B top1Now that the caps are changed out, let’s look at the top of the chassis.  The output transformer and output tubes are on the left side of the chassis.

28V4B top2The preamp tubes and power transformer are at the right end of the chassis.

29V4B top2detail1The open areas around the tube sockets are a nice touch.  The chassis is steel and very stiff, even with the relief.

30V4B top2detail2More low and medium voltage goodness at the other end of the slot.  Nearly every schematic test point is accessible from the top of the unit without turning it over on the bench.

31V4B Magnavox 12DW7This 6K11 Compactron tube tests very good, with each of the sections closely matched to the others.  Good News!

32V4B inputjax1The input jacks were corroded, so these were changed out with new Amphenol units.

33V4B inputjax2Here is the inside-the-chassis view of the new jacks.

34V4B indicator1The neon indicator for the AC power was functional, but the indicator for the high voltage was not.

35V4B indicator2So, this neon indicator will take its place.  The mounting hole is the same size, but the new part is chrome.  What to do?

36V4B indicator3We scrubbed the chrome ring with steel wool, then applied several coats of black polyurethane paint to the bezel.

37V4B Indicator4Here are both indicators.  The high voltage is amber, and the AC indicator is red, as it was when the amp came from the factory.  The colors are a bit messed-up because of the jpeg processing in the camera…  looks good in Real Life!

38V4B Happy CustomerAnother happy customer picks up his finished bass head!

Thanks for reading all the way to the end!

CONTACT – David Latchaw EE
281-636-8626

Peavey Deuce Combo Amp Refurbish

WARNING – A very long blog post awaits you. Typical guitar amplifiers can be described in terms of functional blocks – power supply, preamplifier, power amplifier, and loudspeakers. This refurbishment effort left NONE of those blocks untouched. Sit back and enjoy!

This Peavey needed some work before it could be added to David’s tonal arsenal.

 

I removed the chassis for inspection.  This is the ‘clean’ channel.  The LEDs illuminate to show channel selection.

 

The ‘effects’ channel has a little more tonal control.

 

This unit uses an odd solid state phase shifter scheme and a mechanical reverb unit.  The standby switch is on the front, and the power switch is on the back.  The Fender switch scheme for tube amplifiers sometimes puts both switches in the back, and of course, I always select the wrong one because I have to reach around where I can’t see to work the switch.

 

Somehow, the 8 ohm jack is open-circuit.  We will need to look at this on the inside of the chassis.

 

This is the main power switch.  The ‘ON/ON’ function allows the user to capacitively couple the chassis to one side of the AC line.  This sometimes helps with hum reduction, although the three wire AC cord defeats one side of the switch.

 

The fuse is intact insofar as the red pilot light turns on when power is applied.

 

However, this 10A fuse is the wrong part.  Someone has been jacking with this amp!

 

Sorry, this needs to be fixed.

 

Note that the scratches on the tube base indicate that the tube was inserted incorrectly.  How can this be?

 

This is how.  The guide posts were broken off.

 

The reverb tank bag is screwed down to the bottom of the unit.

 

Everything here is intact, no damage, transducers are OK.  We’ll set this aside in a safe place for now.

 

We found the first bug.  Poor little spider.

 

All of the high voltage capacitors show signs of venting.  See the little bump in the black rubber, next to the 350?

 

The output jacks on the rear of the chassis have been damaged.

 

The pin contact has been bent all the way out so that the plug cannot touch it.

 

This pic is to document that these inside star washers should be placed between the jack and the chassis.

 

Both jacks shall be replaced with new ones.

 

All new hardware was used, of course.

 

The jacks are wired together and the jacks are wired directly to the output transformer.

 

The amplifier circuit board has seen some significant pyrolysis.  Maybe this happened when the tubes were installed the wrong direction, because of the missing guide posts?

 

To remove the amplifier circuit board, the tube socket pins must be unsoldered and the wires removed.

 

With a little attention to detail, the circuit board comes off the tube sockets.

 

This is the underside of the amplifier circuit board.  I wonder if someone poked the wires a little too far, so that the ends touched the chassis?

 

This printed circuit board will be rebuild, and all the components will be moved to the solder side of the board.

 

Lots of rosin flux was used to clean off all the solder.  Lots of alcohol is used to clean off all the rosin flux.

 

The rag gives some place for the mess to go.

 

With the circuit board cleaned up, we can see if it can be repaired.  It’s too old to replace; Peavey has no stock.

 

The carbon tracks are removed.  The remaining copper is trimmed back to where it is still attached to the laminate core.

 

Comparing the circuit board to the layout, we can verify where the traces and components actually should go.

 

Both sides of the circuit board are now spotless.

 

The new components will be placed above the surface of the board to allow for cooling and to insulate each part from the live circuit traces below each component.

 

The copper around the mounting hole is gone, so the lead of this component will be sweat soldered to the surviving trace.

 

To bridge the gaps in the copper, bare solid wire will be soldered in place, and insulated from the rest of the circuit with this Teflon tubing.

 

Here is a picture of the Teflon tubing at work.

 

All of the components are installed now.  The Peavey Deuce uses four 6L6 tubes but only had two screen resistors; the other screens were tied to the plate voltage.  The Peavey Mace amp uses six 6L6 tubes and has six screen resistors.  I went with four screen resistors, as I believe that using two was an engineering oversight.  The original Peavey documentation was ambiguous on this point.

 

This is a nice side view of all the components, flying above the printed circuit board.

 

Subsequent testing showed that the original phenolic tube sockets were either contaminated or were carbon tracked.  The old sockets need to be replaced.  Here, we’re drilling out the pop rivets that hold the sockets onto the chassis.  Note the magnet, which attracts the steel shavings and keeps the mess to a minimum.

 

These tubes hang base side up, thus the base clamps keep the tubes firmly in the socket.  As we know, heat rises, so the sockets get hot during normal operation.  These were cooked.

 

The new sockets will be held in with #8 stainless fasteners.  Here, the chassis holes are enlarged to pass a #8 machine screw.

 

Likewise, the holes in the new ceramic sockets need to be enlarged to the same extent.

 

The sockets will be mounted from the chassis.  We won’t have any access to the bottom of the socket once the printed circuit board is soldered onto the socket pins, so I need some captive hardware permanently mounted to the socket ears.

 

These small outline nuts are brass with a silver plating.  They solder easily to the ears of the new tube sockets.

 

Once the nuts were tacked into position, a nice fillet of solder is run all around the nut to keep them in place.

 

These new ceramic sockets are ready to be tacked into place on the circuit board.  Pay attention to the direction of the index slot!

 

Here are the new ceramic sockets in place on the refurbished amplifier circuit assembly.

 

The new sockets and tube clamps were installed with the stainless steel hardware. To assure that the solder joints under the sockets will not be under stress during operation, a spare octal base tube is plugged into the socket to align the socket contacts before each solder joint on the amplifier pc board is made.

 

Here is the refurbished amplifier circuit board assembly in its final resting place.

 

All the high voltage power wiring, filament wires, and signal wires are in place and ready to be dressed.

 

The power supply circuit board had many bad parts.  The large square resistor seen here was open-circuit!

 

And, when that large resistor died, it got really hot!

 

These large round flameproof resistors are available online as a better-than-factory replacement.

 

Nearly every component on this assembly was replaced.

 

We have 488 volts DC with no load on this assembly.  That will be acceptable.

 

The power supply board is back in place, and the cabling dressed.

 

On the preamplifier board, many of the electrolytic capacitors were showing their age.  The one of the left vented.

 

To remove the preamp board, all the knobs come off (of course.)

 

The felt glued on the face of this socket protect the faceplate from damage.

 

The preamp board is free from its moorings.

 

There appears to be little wrong on this side of the board assembly.  There are no signs of prior repairs here.

 

The vented electrolyte from this electrolytic capacitor attacked the copper lead of this capacitor and ate through it.

 

These cement resistors were bad.

 

The new resistors were mounted off the face of the board, to improve reliability.

 

The controls were flushed, dried, and re-lubricated.

 

This hybrid amp uses solid state techniques for low-level amplification and tubes for high level amplification.  These two transistors were bad.  These driver transistors are part of the phase splitter circuit, and drive the tubes directly.  The replacement transistors have a different pin-out, so the circuit board holes were marked with the correct layout.

 

Some components in the phase shifter circuit were changed out to improve its performance.

 

Here’s one of the original loudspeakers.  Car audio?

 

The other loudspeaker was mildly interesting.  Unfortunately, it was completely destroyed internally and was scrapped.

 

The old loudspeakers were removed and the cabinet was cleared out.

 

The customer selected a pair of import Celestions.  These were modified for an eight-bolt mounting pattern.

 

A magnet was employed to keep the steel shavings away from the loudspeaker magnet.

 

That hand reamer comes in handy to tune up these holes.

 

Here is our loudspeakers in their new home.

 

The loudspeaker wiring on the old speakers was made from microphone cable.

 

We will employ these right angle quarter-inch plugs for the new loudspeaker wiring.

 

The only hard part of using these is getting the solder to tin the case, which is commonly used for the return circuit.

 

We can’t use the cheap stuff now that we’ve gone this far!

 

Sixteen gauge 300v wiring was used for the loudspeaker cables.

 

When assembled, the case forms a clam shell with an integral strain relief.  The extra black wire also serves as a strain relief.

 

Now, all the pieces can be put back together.

 

My favorite part:  First Light from these 6L6 tubes from The Tube Doctor.

 

This thing plays like a new amp.  From 1980.  Because for all practical purposes, it is a new amp from the 80s!

 

Here’s another happy Unbrokenstring Customer!!

 

Thanks for reading all the way to the end!

Contact – David Latchaw EE
Cell – 281-636-8626

My Beer Has A Head – B52 AT100 Head

Chris of Shadow Council told me that his amp head just didn’t sound right after he spilled some “moisture” on top of it. Could the Unbrokenstring Crew take a look and return this amp head to its former metal glory?

Our patient works OK but sounds weak and distorted. Distorted is part of the program, but weak is not.

I think the warranty is out by now, don’t you think?  But I still have these tags on my seat cushions that say “Do not remove under penalty of law.”

A perfect sine wave goes in, and this comes out of the clean channel. We have an issue at or just before the phase inverter circuit.

Let’s look around inside the amp.  At this end of the front panel, we have the power switches and pilot light.

From left to right are the master reverb and master volume controls, and the controls for the CLEAN channel.

The yellow rectangular parts are relays for channel and mode switching.

There are a lot of controls for the OVERDRIVE channel.

I really like the separate circuit board for the input jacks.  This makes servicing the jacks very easy.

Shifting our attention to the rear of the chassis, we see the power amp circuit board at the bottom of the picture.  At the top of the picture is the effects loop send/return jacks and level controls.

At the top of this picture is the rest of of the effects send/return jacks circuit board, with level controls and the foot switch jacks at this end.

The circuit assembly on the left is a ‘Line Out’ jack with its own level control.  The cluster of wires in the middle go to a loudspeaker cabinet impedance selector switch.

Another nice feature is that the output jacks are on their own circuit board, making service easy.  Can you spot the overheated resistor in this picture or in the previous picture?

On the left is the Rectifier Selector switch.  A half-wave tube rectifier circuit, a full wave tube rectifier circuit, or a solid state rectifier circuit can be selected here.  The AC line cord is on the right.

Note that the black plug for the reverb tank goes to the red jack, and the red plug goes in the white jack.  Think about it.

The chassis is out of the case.  Let’s do some tests!

The final amp circuit board has been pivoted up out of the way in order to check circuit wave forms.  Fortunately, the tubes don’t need to be ALL the way in the socket in order to do some tests.  This tube had a bent pin, and I didn’t force it into the socket.  Easy to fix with the power off.

The problem is somewhere around the third socket from the left.  I wonder what’s going on with the contamination?  Beer?  Whiskey?  Probably not vodka.

A pink rag is catching the junk floated off the circuit board with this pressurized circuit board de-fluxer product.

A vacuum tube voltmeter showed that portions of the high impedance circuits around this tube were upset by gunk under the tube socket.

The socket has plenty of gunk of its own and will get cleaned up with solvent and a brush.

Here we see the circuit board underneath the socket.  Some of the residue is conductive and has upset the circuit operating voltages.  But look to the left at the base of the next socket.  See anything?

This socket has been removed as well.  Can you see it?

The Xacto knife points to a trace in the circuit board that has disappeared.

The entire board was scrubbed, sockets were cleaned, and reassembled to the circuit board.  The blue wire bypasses the open-circuit section of the burned printed circuit board we spotted earlier.  This section of the tube amplifies a LOT better when the plate terminal is hooked up to the following stage.

A pair of low value resistors serve as fuses in the high voltage plate circuit.  Component RX is toast.

While we have the amp apart, we can fix the loose knob cover on the “Rectifier Select” switch.

Old glue residue was removed from these parts.  Super Glue is just the ticket for this sort of thing.

If you don’t get it on your fingers, the Krazy Glue works well.  Don’t ask me about the fingers, please.

Now that everything is working, a protective coating will be sprayed over the top of the circuit board to keep ‘moisture’ away from the live circuits.  Each tube socket (and anything else we don’t want coated) is masked off.

This circuit assembly is masked and ready for coating.

Today we will use this commercial/industrial silicone conformal coating.

The spray pattern looks about like this.  I think we’re ready to go.

The circuit board gets four coats.  Each coat is sprayed from a different direction (top, bottom, left, right) to build up a uniform protective coating.  The coating ‘conforms’ to the shape of the circuit board, thus the name “conformal coat.”

I let this cure for a couple of days.  Now bring on whatever “moisture” you want to spill into the top of the cabinet!!

As you can see here, we’re peeling off the masking tape.

Red on white, black on red…  or something like that.

The tube base clamps were cleaned up, ever-so-gently bent back into position, and installed.  These machine screws hold the circuit board to the bottom of the chassis.

All the wiring is reinstalled where it came off.  I take a lot of pictures because my memory may not be perfect.

Just about done with reassembly.

The tubes were in excellent electrical condition. They all go through the tube pin straightener before they are re-installed.

You saw these jacks in an earlier picture.  I took the opportunity to clean and lubricate all the jacks while the amp was apart.

Ah, that’s more like it.  This is a 400Hz sine wave amplified to about 110 watts into a non-inductive high-power resistor.  The bias current to establish Class AB1 operation is just about perfect, judging by the zero-crossing points on this waveform.  Attached to any decent cabinet, this amp would be melting our teeth at this power level.

Support this local band!

Thanks for reading all the way to the end!

Contact – David Latchaw EE
Cell – 281-636-8626

Fender Hot Rod Deville Makes Funny Noises!

Matt from My Twilight Pilot told me that his wonderful Fender Hot Rod DeVille had developed some strange noises.  The volume control was really too sensitive, no low end audio, audio clipping, and we were experiencing some general shakes, rattles, and rolls.  Could the Unbrokenstring Crew help?

Finally, an appropriate warning label…

This brand new tube chart clearly shows that this is one of the wonderful reproduction units from Fender.

Service literature is easy to get from Fender for this model.

The treble tone cap was replaced with a silver mica unit (already installed.)

The bass tone cap on the right was replaced with the orange film cap on the left.  The larger size buys us some reliability as the internal dielectric is a little thicker, a good then when operating at a plate voltage of 350 volts.  The mid-range tone capacitor was also replaced with another orange CDE cap of the proper value.

The tone stack capacitors are now soldered in.  The leads will be trimmed and the rosin flux will be cleaned off.

When the signal generator was swept through the audio range, a mechanical rattle was heard in the vicinity of the reverb tank.  I’ll loosen the reverb tank and do the test again.  This thing IS loud!

A quick check of the electrical connections shows that everything is as it should be.  But the rattle remains!

The loudspeakers are a little loose, but no rattle here.

Aha!  It’s the bottom of the baffle board.  All the bolts were loose.  Here they are re-torqued to about 5 ft-lbs.

A fresh set of output tubes were run for four hours and re-biased per Fender specs.  A 12AY7 was installed in the first preamp.  This tube has lower gain than the 12AX7 used at the factory.  This change gives a little more ‘spread’ to the volume control, increasing its usefulness.

This is a view seldom seen unless you are in the business!  Nice lead dress.

To do the full-power tests, the window is opened and the amp is turned around.  Yes, this is VERY LOUD!  And quiet when it should be.  My job here is done.

Support this local band!

Thanks for reading all the way to the end!

Contact – David Latchaw EE
Cell – 281-636-8626

Fender Bassman Blackface Amp s/n 73 Refurbishment

The call came in from an individual who had ‘this old guitar amp’ that didn’t work.  They wondered if The Unbroken String Crew could get it playing for the grandchildren.  I was not ready for what I saw when they dropped it off.

This Fender Bassman was absolutely original. I could not tell that anyone had ever worked on it except for a couple of new tubes.

Everything was original, with some signs of wear and tear as you might expect to find after fifty years. Only the speaker cable was aftermarket.

Nothing came on when power was applied. This may be Pandora’s Box.

Let’s take a look inside. Not many people have ventured to this point in guitar amplifier space and time. Come join me as we go exploring!

The tube chart is obviously original, with the serial number hand-stamped as you see here. WOW!

Let’s take a look at that fuse.

What do we have here?  I’ve not seen a fuse like this since I left Oklahoma.

This is vintage Wrigley’s Chewing Gum aluminum foil, wrapped around a stick. One end of the aluminum has burned away.  Mojo Toan…  NOT!

The original two-wire line cord has been VERY hot. This line cord will be replaced with a three wire IEC cord set to bring this amp up to code, as it were.

This is a good reason to have a fuse in your AC power. This penny was rolling around inside the amp chassis. Don’t you just love grandkids?

Let’s take a chassis tour and enjoy a bit of history.  Here is the power transformer, power tubes, a bias balance potentiometer (more on this later) and a separate turret board that holds the solid state rectifiers and a separate power supply for tube bias.  The pilot light is visible in the upper left hand corner of this picture.

On this end of the chassis, we see the preamp tube sockets and the entire turret board.  The brown paper capacitors are dual section capacitors, as they have three legs.  These are over fifty years old, but will be changed out on general principle.

Here is a closer look at the solid state rectifiers, bias power supply, and pilot light.

These front panel controls are the bass, treble, and volume for the normal channel, and a slide switch labelled “BRIGHT.”  The control mounted on the pan of the chassis is a ‘bias balance’ control, which is set for minimum hum.  No, this does not adjust the bias per se.  We will adjust this after the new tubes are installed.

The two normal input jacks are in the center of the pic.  This is a good shot of the traditional Fender brass grounding strip found behind the control panel.

These are the controls for the bass channel, the DEEP slide switch, and the bass input jacks.

Not much on the rear panel behind the preamp tubes, but you can take a good look here at the nice workmanship and component quality shown throughout this amp.

From this view, you can see the output jacks, the power switch, and the standby switch.

To the right of the fuse holder, you see the ground switch and a convenience outlet.  The ground switch will be problematic with the three-wire-cord conversion, because only the green wire ground in the power cord can go to the chassis, whereas with the two prong cord system, the AC hot wire can be connected to the chassis through this switch and a single capacitor.  If the capacitor fails, people die from electrocution.  I’ll show you a solution if you keep reading.

To remove the old power cord, the strain relief grommet is compressed with some heavy pliers.

We will keep this grommet for reuse with the new IEC cord set.

 

The old cord gets now gets cut away from the convenience outlet.

To simplify rewiring the AC circuit, I’ll pull the convenience outlet.

The wire used in this amp is bare wire, with a yellow ‘push-back’ insulation. I’m saving all the original wiring and will reuse it in the new AC circuit.

Now I’m removing the ground switch, to facilitate rewiring it into a ground-lift switch.

Everything is out where I can work on it.

The black wire is the ‘hot’ lead to the power transformer and the white wire is reserved for the neutral leg.  Can you see the error?  Black wires should be on brass screws.  In the early days of residential AC power, either prong of the power cord could be hot.  But in this century, the brass screw has been reserved for hot and the silver screw has been reserved for neutral.  This is easy enough to correct.

The Fender Death Cap is connected to the chassis here.  It needs to come out, because if it shorts, the chassis becomes electrically hot and WILL electrocute anyone touching it or connected to it (read: guitarist.)  Not Cool!

The Fender Death Cap is hidden down in the wiring.  Out it comes!

This is a better view of how it is attached directly to the chassis.  I would have just cut the wire, but I want to reuse this hole and connection point for the green wire ground connection.

You don’t see this sort of thing anymore! Not made is USA, but made in the U.S. ‘Cuz this is ‘Murica!

Now, we are ready for the new line cord, sporting the recycled strain relief grommet.  We’re about done here.

If you were sharp-eyed, you probably noticed the cathode bias resistors attached to the bottom of the tube sockets. Here is a good view.

Do you see the cooked resistor on the socket of the tube? That was the cathode bias resistor. Somewhere along the line, a tube failed and overheated this resistor.

The burned resistor measured about two hundred ohms.  This really upsets the operating point of whatever tube works out of this socket.  Tough duty!

I will change out both parts so that both circuits can stay matched. A pair of new resistors will have the same initial value, will behave the same over temperature, and will age in similar manner.

These new flame-proof resistors are considerably tougher than the carbon composition resistors they replace.

The high voltage filter capacitors are located under this pan.

The outer cardboard tubes have been rotated to verify the values and voltages of each component.

The capacitor on the left has vented.  The bulges on the other capacitors show that they are near end of life.

They are all ready to pop and make a mess.

These are German-made high temperature, long-life capacitors.  I consider these to be equal or better than the originals.

With the new caps installed, a power-up test shows a healthy 279 volts (unloaded) for the tube plates.

I think our work here is done.  The external appearance of the amp is not altered, so substituting those after-market high voltage capacitors will be our little secret, OK?

One last repair…  Every control is scratchy.  Those little slots you see on these controls is (1) an opportunity for dirt to get inside the control, and (2) an access point to squirt some tuner cleaner.  After squirting some cleaner in these controls, they were still scratchy.  I don’t want to change out the controls because the new stuff is not nearly as good as these 50 year old parts, and I don’t want to diminish the value of this amp.  Time for surgery!

Each control was de-soldered, removed from the front panel, and disassembled.  This old stuff is service-able, unlike the mass-produced controls built by the ChiComs today.

The shaft is grounded to the mounting bushing, and the back cover is grounded to the chassis because the shaft rubs on a spot in the middle of the back, as shown.  Old grease and oxidation has been removed, and a tiny drop of synthetic lubricant will be smeared at this point of the rear cover.

The shaft jammed inside the bushing.  A little judicious filing burnished the shaft where it had been scarred by the knob set screws.

Here again, we find fifty years of oxidized grease and dirt.

You can see several sliding contact points between the actual resistive element and the outside world.  On the right, the dark ring is the actual resistor.  The thin copper ring in the center forms a connection between the resistor slider that floats over the resistive element and the middle (wiper) terminal of the potentiometer assembly.  On the right, we see the brass slider, fastened to the shaft and knob.  All the metal components are now burnished.  The resistive element in this style of potentiometer is fairly tough, so it will get a burnishing with a cotton swab.  DO NOT ATTEMPT to touch the resistive element in any modern potentiometers, as they are thin films and irreparably damaged by the smallest unseen scratch or sleek.  You Have Been Warned.

Everything gets reassembled with synthetic electronic spray lubricant and reassembled.  Here, we’re making a quick check of the operation of the control before it gets reinstalled (and we go on to the next one…)

Each control is reconditioned in sequence.  This is going to be a long night!

Earlier, I showed pictures of a ‘bias balance’ control.  This control does not set the bias point of both tubes, but rather balances the idling current through both tubes.  The factory adjustment literally says, “Adjust the control for minimum hum.”  And it works.  For the Tubeheads out there, the minimum hum point in this particular amp leaves each tube idling at 35.2mA of plate current.  This is also why the cathode resistors need to be matched.  But the tubes characteristics can vary a bit, and the balance control allows the tech to compensate for that variability.  See my tube bias jig under one of the output tubes?

Before we reassemble this guy, let’s take one last look at the definition of hand-crafted 1960’s American electronics. Just gorgeous!

Not only will the grandkids have access to a nice amp, but this bit of history will hold its value for many years to come. Thanks for the opportunity to refurbish this wonderful bit of history.

And thank you for reading all the way to the end!

 

CONTACT – David Latchaw EE

281-636-8626