Peavey Citation MK IV Two Channel Guitar Amp Head Repair

Rod had this Peavey head kicking around and thought it was time to put it to good use. However, it didn’t work at all. Could the Unbrokenstring Crew work its magic and bring this road warrior back to life?
A quick scan of the front panel shows that the input circuit sports the sort of flexibility that the Peavey Marketing Department loves to explain to anyone who would listen…
Each channel has independent gain, and a master volume to Rule Them All.  Effects can be inserted via the front panel.
On the rear panel, we have parallel speaker jacks and the usual ground/no-ground power switching.  Peavey often married different front panels, which contained preamp circuitry, to different rear panels, which carried power and audio amplifier components.  The ‘series’ number goes with the power amp, not the front panel.  We Got This.
Name, rank, and serial number, please.
Pulling the front panel, we see that all of the components are mounted on one circuit board.
I took a few pictures to be sure that the wiring and cables were returned to the same spot when we are through.
The cable to the right is just wired to the power indicator.  The other two carry signals.
This is a better view (to be sure that they cables are properly oriented on their pins.
The front panel is free of the rest of the unit.
All of the controls and switches will be cleaned so this assembly comes completely apart.
We can now clean and lubricate everything now.

 

Can you spot the broken solder joints?
Someone has been here before!  This needs to be cleaned up, too.
The Blue Shower is a good cleaner.  The DeoxIt contains a lubricant for the potentiometers.  Good Stuff!
Back Together it all goes!
This screw hole was stripped out.  First, we will soak the stripped hole in the wood with this wood hardener.
Next, a birch dowel is cut to partially fill the hole.  The dowel reduces the apparent diameter, allowing the screw to hold.
With the stripped hole repaired, we are back in business!
This unit plays very well, and all the controls and switches are Like New!

 

Thanks for reading all the way to the end!

CONTACT – David Latchaw EE
281-636-8626

Blackstar HT5RH Guitar Head is Dead

This five watt head had gone nearly silent. The national retail chain that sold it told the owner to purchase a new one, because that’s their business model. Could the Unbrokenstring Crew repair this unit and bring it back to life?

At five watts, this head is bedroom-friendly, yet there are plenty of opportunities for distortion and tone shaping.

 

Interestingly, there are three options for outboard speaker cabinets as well as all of the usual in’s and out’s.

 

The back comes off with these screws.  But it appears to be stuck in place!

 

I speculate that when the unit was built, the Tolex glue was still fluid and squeezed out between the back and the frame, sticking the rear cover in place.

 

The chassis is held in with these screws.  No surprises here.

 

This is a hybrid solid state / tube unit, with a 12AX7 triode pair in the preamp section and a dual triode 12BH7 pressed into service as a push-pull tube output stage.

 

There are two different versions of the schematic available.  They can be easily identified by checking the number of conductors in that big ribbon cable that connects the rear panel circuit board to the main circuit board.  This particular unit uses the cable with 21 conductors.  Thanks to Armando Garcia at Mars Electronics who furnished this schematic!

 

In the foreground are the big heat sinks for the voltage regulators.  The rear panel wiring board is in the background.

 

Viewed from the other side, the main circuit board contains the preamp circuitry.

 

The preamp uses DSP techniques to create the reverb effect and the tone-shaping functions of this unit.

 

This is the preamp tube.  It’s fine.

 

This is the 5 watt output tube.

 

This part checked OK but it is a little weak.  We will continue to use this unit for troubleshooting purposes.

 

This is the pin-straightener from my tube tester.  The Chinese tubes have a little larger envelope than the JAN versions of these tubes, so the tube is a tight fit in the straightener.  If the tube envelope is too large, the pins can be straightened using the same tool, but the pins are inserted from the other side of the straightener.

 

So the output drive signal is split into an in-phase and out-of-phase copy, and applied to the grid of the output tube.  But the plates of the 12BH7 are stuck at +300 volts.

 

The primary windings of this output transformer are shorted to each other.

 

Let’s get this transformer off the chassis and take a closer look at it.

 

These Chinese transformers are usually not worth fixing, but this transformer is hard to find.  Some exploratory surgery shows us that the problem is deeper in the windings and not readily repairable.

 

So, out it comes entirely.  The search is on for a replacement.  The original manufacturer has no stock.

 

Hammond makes a versatile aftermarket unit that is available through distribution.  We can make this work!

 

The frame of the transformer is just a little bit larger than the original part.  One of the mounting holes is being moved.

 

Placing the magnet near the site where the drill is working helps keep those pesky metal shavings under control.

 

The new transformer is bolted in place and some Thread Locker is applied to the bolts to keep it in place.

Here the output leads are threaded through the insulating grommet in the chassis.

 

The input wiring is soldered into place, so the leads are trimmed to length.

 

To preserve the original wire insulation colors silkscreened on the circuit board, short pieces of the original wiring were left in place and butt-spliced to the new output transformer harness.

 

This unit is ready to test.  Pretty neat looking!

 

Surprisingly, this unit has a bias pot and a balance pot.  However, there is no commonly-available information available for the technician to set these.  So, I wrote this procedure:

BALANCE ADJUSTMENT

  1. Set DMM to mV range
  2. Affix DMM probes to TP6 and TP7
  3. Switch POWER ON; switch STANDBY ON after five minute warmup.
  4. Adjust BALANCE pot for 0V display on DVM
  5. Switch all power OFF

BIAS ADJUSTMENT

  1. Affix black DMM lead to ZD2 cathode (banded end) near Input Jack. This is a convenient GND.
  2. Affix red DMM lead to D20 anode (not banded end.)
  3. Switch POWER ON; switch STANDBY ON after five minute warmup.
  4. Adjust BIAS pot so that DMM display is 46mV.  This puts about 10mA of idle current through the 12BH7.

Recheck BALANCE and BIAS adjustments as they are slightly interactive, particularly if the internal sections of the 12BH7 tube are not matched.  Follow all the usual precautions of removing power and working safely around high voltage!

Thanks for reading all the way to the end!

CONTACT – David Latchaw EE
281-636-8626

Ashdown EVO II 300 Bass Head Repair

This British-made bass head was dead to the world.  After looking at the fuses, nobody would dare open it for service, possibly because there was no service literature available in this hemisphere, or perhaps out of reverence for the brand.  This is a hybrid amplifier, with a tube in the preamp chain and a solid state power amplifier.  Would the Unbrokenstring Crew run where angels fear to tread?

01ASH the patientThe owner said that he would clean up the front panel.  Just get the thing working.

02ASH backsideThe steel chassis was just the ticket to keep everything in its place.  You can see the Trace Elliot heritage in this brand.

03ASH back closeHere’s a close-up of the rear panel.  The footswitch must have a pair of switches and a pair of quarter-inch plugs.  The line input jack is an interesting feature.

04ASH chassis scrThese plastic caps covered the screws that secured the chassis to the case.  Well, it appears someone has been here before us!

05ASH scrA little care and a #3 Phillips was enough to bite into these screws and get the unit open.

06ASH power supplyHere, the power amp board is pulled free for inspection.  That’s some big wire!

07ASH cookedCan you see the failed solder joint?  The four elongated tabs are the terminals on a large full-wave bridge rectifier.

08ASH repairEach of the solder joints were de-soldered and then re-soldered with fresh solder.  The joint that failed may have been on an ever-so-slightly thinner trace, so a jumper wire adds some circular mils of copper to that part of the circuit to keep the temperature rise of the circuit board down.

09ASH on the airBehold!  Everything comes alive!  This meter is really a nice-looking feature.

10ASH finishedThis unit is conservatively rated at 300 watts.  The unit barely got warm after four hours at that power level.  I think we fixed it!

Thanks for reading all the way to the end!

CONTACT – David Latchaw EE
281-636-8626

Pignose 7-100 Mini-Amp Refurb

This battery-powered portable amplifier is a novelty item seen in offices, bedrooms, and showrooms around the country.  This little guy doesn’t work anymore.  Could the Unbrokenstring Crew make it work again?

01PIG the patientThe pig’s nose is the on-off/volume control.  The input jack is just below the nose.

02PIG insideInside, we find a loudspeaker and battery box on the left, and the electronics and some cord storage on the right.

03PIG missing nutThis nut is missing.  Oh boy, this is Big Trouble in Little China.

04PIG acid everywhereThe cover over the electronics shows signs of corrosion, probably from battery acid.

05PIG found nutGood news!  We found the missing nut.

06PIG jacksThis panel is on one side.  Surprisingly, the power jack is ‘old technology’ and probably should be the same connector as seen on effect pedals.  But, hey, they didn’t ask me.

07PIG nameRankSerialThis metal piece secures the battery boxes in place.  Name, rank, and serial number please.

08PIG new bat boxThe original battery box was trash, so these units were procured.  Six batteries give us nine volts.  These x3 packs are necessary to fit into the space provided.

09PIG acid here tooCaustic chemicals from the leaking batteries were conducted, via capillary action, over to the amplifier side of the box.  A new pair of red and black wires were fished through the umbilical, replacing the corroded wires.

10PIG wired boxesHere, the new battery boxes are wired into the unit’s harness.

11PIG fitting boxesThe battery boxes rest on a metal bracket, which also serves as a noise shield over the volume control and input jack.

12PIG Strain reliefThis grommet serves as a strain relief for this end of the umbilical cable.

13PIG looking goodThis pic just shows how the leads are dressed. This unit is small, and the wires need to go into their correct places in order to close the unit up when we’re through.

14PIG watch lead dressThese red and black wires can be pinched between the case and the metal plate, so they need to be pulled up and out of the way before the screws are tightened down.

16PIG clean ampWe find the preamp and amp in the other side of the unit. The small assembly seen at the bottom is back side of the power jack and the ‘preamp out’ jack.

17PIG reinstall ampThis assembly was covered with caustic chemicals from the leaked batteries.  Miraculously, these transformers were not damaged.  Everything cleaned up very well.

18PIG cover onThis cover shields the amp and jacks.  We’re done here.

19PIG batteriesA fresh set of batteries and a twist of the knob puts this unit back on the air.  Time to call the customer!

Thanks for reading all the way to the end!

CONTACT – David Latchaw EE
281-636-8626

Ampeg SVT-200T Bass Head Update to IEC AC Power Entry

This absolutely mint-condition solid state bass amp head came through the shop for a quick once-over.  More significantly, the owner wanted one of those new-fangled IEC AC power jacks installed in place of the existing power cord.

01SVT the patientThese units are highly regarded by many bass players.  Some consider them to be an equal to the tube-based models in the realm of versatility and sound.  And they are sure a lot lighter to carry around!

02SVT line outsThe rear panel is straight forward, with everything you need for a decent bass amp setup.  More goodness from St. Louis Music Electronics!

03SVT amp1Inside, we have the interface to the front panel and some power transistors.  The unit with two flag terminals is a thermal switch that opens when the heat sink gets too hot.

04SVT amp2Here we have more power transistors and the driver transistor pairs.

05SVT amp3Power supply capacitors and the choke are found on this end of the board.

06SVT amp4The power transformer is bolted here, and the input protection circuit board is mounted on the side of the chassis.

07SVT fp1Input jacks and controls are found in this view, facing the back of the front panel.

08SVT fp2This is the rest of the front panel.  Note the big solid state rectifier for the power supply in the center foreground.

09SVT technologyAmerican-made Texas Instruments semiconductors are widely used throughout this unit.  Here is a preamp chip.

10SVT cordThe original line cord is removed with a snip.  The wire remaining inside the chassis will be soldered directly to the IEC connector.  The big chunk of insulation will be removed.  The AC wiring will then be dressed in the same manner as the rest of the under-chassis wiring.

11SVT pwr inThis blue IEC connector will be installed in the rear panel where the strain relief bushing goes.

12SVT hole dimsA rectangular hole will be cut to mount the IEC connector.  The pencil lines show up pretty well in this view.

13SVT magnetA magnet is positioned to keep the metal chaff from the sheet metal nibbler away from the electronics.

14SVT holeThis is the rough-cut hole.  More filing will gun-smith this into a rectangular shape.  Note the handle on the magnet visible through the rectangular hole.

15SVT trial fitHere, we are trial-fitting the IEC connector.

16SVT screwholeThe location of the hold-down screws is marked with a center punch.

17SVT drillNow the holes for the screws are drilled, as you might have guessed.

18SVT trilobed scrThe machine screws are torqued, mounting the IEC connector in its new home.

19SVT magnetsThe magnets have really done their job.  None of these filings will be left loose inside the chassis!

20SVT wire prepThe cut ends of the power cord inside the chassis are stripped and tinned.

21SVT shrinkAs a nice touch, some heat shrink tubing of the correct color is slipped onto each wire.  Pure cosmetics!

22SVT solderThese are tacked into place for now.  Before the final joint is made, I’ll verify that the wires go to the right place!

23SVT shrinkWiring orientation is confirmed as correct!  The soldering was completed and the heat shrink tubing is shrunk into place.

24SVT line out testHere, I’m checking the functionality of the low-level signals to feed a bi-amp setup.  Note the Marshall Stack!

25SVT final testThis unit is ready for the 21st century.  The modular cord makes setup and transportation more convenient.

 

Thanks for reading all the way to the end!

CONTACT – David Latchaw EE
281-636-8626