Ashdown EVO II 300 Bass Head Repair

This British-made bass head was dead to the world.  After looking at the fuses, nobody would dare open it for service, possibly because there was no service literature available in this hemisphere, or perhaps out of reverence for the brand.  This is a hybrid amplifier, with a tube in the preamp chain and a solid state power amplifier.  Would the Unbrokenstring Crew run where angels fear to tread?

01ASH the patientThe owner said that he would clean up the front panel.  Just get the thing working.

02ASH backsideThe steel chassis was just the ticket to keep everything in its place.  You can see the Trace Elliot heritage in this brand.

03ASH back closeHere’s a close-up of the rear panel.  The footswitch must have a pair of switches and a pair of quarter-inch plugs.  The line input jack is an interesting feature.

04ASH chassis scrThese plastic caps covered the screws that secured the chassis to the case.  Well, it appears someone has been here before us!

05ASH scrA little care and a #3 Phillips was enough to bite into these screws and get the unit open.

06ASH power supplyHere, the power amp board is pulled free for inspection.  That’s some big wire!

07ASH cookedCan you see the failed solder joint?  The four elongated tabs are the terminals on a large full-wave bridge rectifier.

08ASH repairEach of the solder joints were de-soldered and then re-soldered with fresh solder.  The joint that failed may have been on an ever-so-slightly thinner trace, so a jumper wire adds some circular mils of copper to that part of the circuit to keep the temperature rise of the circuit board down.

09ASH on the airBehold!  Everything comes alive!  This meter is really a nice-looking feature.

10ASH finishedThis unit is conservatively rated at 300 watts.  The unit barely got warm after four hours at that power level.  I think we fixed it!

Thanks for reading all the way to the end!

CONTACT – David Latchaw EE
281-636-8626

Pignose 7-100 Mini-Amp Refurb

This battery-powered portable amplifier is a novelty item seen in offices, bedrooms, and showrooms around the country.  This little guy doesn’t work anymore.  Could the Unbrokenstring Crew make it work again?

01PIG the patientThe pig’s nose is the on-off/volume control.  The input jack is just below the nose.

02PIG insideInside, we find a loudspeaker and battery box on the left, and the electronics and some cord storage on the right.

03PIG missing nutThis nut is missing.  Oh boy, this is Big Trouble in Little China.

04PIG acid everywhereThe cover over the electronics shows signs of corrosion, probably from battery acid.

05PIG found nutGood news!  We found the missing nut.

06PIG jacksThis panel is on one side.  Surprisingly, the power jack is ‘old technology’ and probably should be the same connector as seen on effect pedals.  But, hey, they didn’t ask me.

07PIG nameRankSerialThis metal piece secures the battery boxes in place.  Name, rank, and serial number please.

08PIG new bat boxThe original battery box was trash, so these units were procured.  Six batteries give us nine volts.  These x3 packs are necessary to fit into the space provided.

09PIG acid here tooCaustic chemicals from the leaking batteries were conducted, via capillary action, over to the amplifier side of the box.  A new pair of red and black wires were fished through the umbilical, replacing the corroded wires.

10PIG wired boxesHere, the new battery boxes are wired into the unit’s harness.

11PIG fitting boxesThe battery boxes rest on a metal bracket, which also serves as a noise shield over the volume control and input jack.

12PIG Strain reliefThis grommet serves as a strain relief for this end of the umbilical cable.

13PIG looking goodThis pic just shows how the leads are dressed. This unit is small, and the wires need to go into their correct places in order to close the unit up when we’re through.

14PIG watch lead dressThese red and black wires can be pinched between the case and the metal plate, so they need to be pulled up and out of the way before the screws are tightened down.

16PIG clean ampWe find the preamp and amp in the other side of the unit. The small assembly seen at the bottom is back side of the power jack and the ‘preamp out’ jack.

17PIG reinstall ampThis assembly was covered with caustic chemicals from the leaked batteries.  Miraculously, these transformers were not damaged.  Everything cleaned up very well.

18PIG cover onThis cover shields the amp and jacks.  We’re done here.

19PIG batteriesA fresh set of batteries and a twist of the knob puts this unit back on the air.  Time to call the customer!

Thanks for reading all the way to the end!

CONTACT – David Latchaw EE
281-636-8626

Ampeg SVT-200T Bass Head Update to IEC AC Power Entry

This absolutely mint-condition solid state bass amp head came through the shop for a quick once-over.  More significantly, the owner wanted one of those new-fangled IEC AC power jacks installed in place of the existing power cord.

01SVT the patientThese units are highly regarded by many bass players.  Some consider them to be an equal to the tube-based models in the realm of versatility and sound.  And they are sure a lot lighter to carry around!

02SVT line outsThe rear panel is straight forward, with everything you need for a decent bass amp setup.  More goodness from St. Louis Music Electronics!

03SVT amp1Inside, we have the interface to the front panel and some power transistors.  The unit with two flag terminals is a thermal switch that opens when the heat sink gets too hot.

04SVT amp2Here we have more power transistors and the driver transistor pairs.

05SVT amp3Power supply capacitors and the choke are found on this end of the board.

06SVT amp4The power transformer is bolted here, and the input protection circuit board is mounted on the side of the chassis.

07SVT fp1Input jacks and controls are found in this view, facing the back of the front panel.

08SVT fp2This is the rest of the front panel.  Note the big solid state rectifier for the power supply in the center foreground.

09SVT technologyAmerican-made Texas Instruments semiconductors are widely used throughout this unit.  Here is a preamp chip.

10SVT cordThe original line cord is removed with a snip.  The wire remaining inside the chassis will be soldered directly to the IEC connector.  The big chunk of insulation will be removed.  The AC wiring will then be dressed in the same manner as the rest of the under-chassis wiring.

11SVT pwr inThis blue IEC connector will be installed in the rear panel where the strain relief bushing goes.

12SVT hole dimsA rectangular hole will be cut to mount the IEC connector.  The pencil lines show up pretty well in this view.

13SVT magnetA magnet is positioned to keep the metal chaff from the sheet metal nibbler away from the electronics.

14SVT holeThis is the rough-cut hole.  More filing will gun-smith this into a rectangular shape.  Note the handle on the magnet visible through the rectangular hole.

15SVT trial fitHere, we are trial-fitting the IEC connector.

16SVT screwholeThe location of the hold-down screws is marked with a center punch.

17SVT drillNow the holes for the screws are drilled, as you might have guessed.

18SVT trilobed scrThe machine screws are torqued, mounting the IEC connector in its new home.

19SVT magnetsThe magnets have really done their job.  None of these filings will be left loose inside the chassis!

20SVT wire prepThe cut ends of the power cord inside the chassis are stripped and tinned.

21SVT shrinkAs a nice touch, some heat shrink tubing of the correct color is slipped onto each wire.  Pure cosmetics!

22SVT solderThese are tacked into place for now.  Before the final joint is made, I’ll verify that the wires go to the right place!

23SVT shrinkWiring orientation is confirmed as correct!  The soldering was completed and the heat shrink tubing is shrunk into place.

24SVT line out testHere, I’m checking the functionality of the low-level signals to feed a bi-amp setup.  Note the Marshall Stack!

25SVT final testThis unit is ready for the 21st century.  The modular cord makes setup and transportation more convenient.

 

Thanks for reading all the way to the end!

CONTACT – David Latchaw EE
281-636-8626

Fender Hot Rod Deluxe Car Wreck

This seasoned road warrior was happily touring and now was called up for recording duty.  However, at the final live set, the unit became very warm and the audio dropped way off.  Could the Unbrokenstring Crew work some magic to return this guy to the studio?

01HRD the patient1This unit has been in the shop once in the last year for a defective plate load resistor in the phase inverter.

02HRD nameplateApparently Fender received a batch of defective plate load resistors. The vendor corrected the problem, but a few of the amplifiers built with that particular batch of resistors have been in the field for years.

03HRD take apartThe circuit boards need to come loose to access everything. It turns out, the heat is coming from several sources.

04HRD probingThe schematic is on the monitor.  Unbrokenstring is trying out the Paperless Office Experience.

05HRD the problemThis is one of the open-circuited plate resistors on the phase splitter tube.

06HRD FixedHere is an NOS carbon composition resistor from stock.  It looks right at home in this amp.

07HRD caps1The real issue today is that the capacitors have begun to vent.  We need to address this with a recap.

08HRD caps2These units are all on the same circuit and are all the same age.  So they are all to be replaced.

09HRD heat1A previous non-Unbrokenstring repair around the low voltage regulator circuits fixed some burned circuit boards.

10HRD heat2These large resistors limit the Zener current. They are too close to the printed circuit board.

11HRD temp rangeThe capacitors will be replaced with units that have a higher temperature rating.

12HRD new partsHere, the Zener diodes and power resistors are spaced above the circuit board for better ventilation.

13HRD teflon tubingSome amp techs touch each cap with a screwdriver to discharge them. The positive lead carries about 400vdc and represents a safety hazard.  Those who ‘know’ will use a discharge wand on the tube socket or choke terminals to discharge this high voltage.  For the screw driver’s sake, we’re installing Teflon tubing on the exposed high voltage points.

14HRD plate resistor1We are changing out the plate load resistors.  All of the preamp tubes use a 100k resistor in the plate circuit.  This resistor is also part of the audio path e.g. the amplified signal appears on the plate end of this resistor, so we will benefit from modern 21st century components for duty in this part of the circuit.   Again, they are spaced above the circuit board to keep the body temperature (and noise) low.

15HRD plate resistor2More plate load resistor goodness…

16HRD input jacks1The plastic input jacks are replaced with American-made Amphenol units which are bolted directly to the front panel.

17HRD first testThe circuit boards are placed back into position and the unit is placed under test.  After an hour and a half of a four hour burn-in, the amplitude dropped off again.

18HRD power1Bias current climbed a few milliamps and could not be put back to normal. Here is a temperature reading at the base of one of the output tubes.

19HRD power2This is the temperature of the other tube base.  Obviously, the circuit is unbalanced now because the other tube is a lot hotter.  We will check the tubes again, but something else is happening here.

20HRD preampHere is the temperature of one of the preamp tubes.

21HRD transformersSurprisingly, everything returns to normal when the amp cools.  The chassis is on the bench now to take a closer look.  Something looks wrong with the output transformer.  Running the unit on the bench while applying a heat gun to the output transformer duplicated the problem!

22HRD disassembly againA new output transformer is still available from Fender!  Let’s substitute the new one and restart the test.

23HRD wires1The red and brown leads are the ends of the output transformer primary winding that are driven by the output tubes.

24HRD wires2The red wire is the center tap, which is fed high voltage.  The black wires connect the power supply choke into the circuit.

25HRD wires3The output windings of the output transformer go here.  Pay attention to the striped, unstriped, and black wires.

26HRD wires4All of the wires to the output transformer go through this TieWrap.  We’ll snip this to get it out of the way for now.

27HRD wires5Here are the output transformer leads.  Now, we unscrew the transformer from the chassis.

28HRD xformer1I compared the two transformers.  The bases are lined up, but the top is misaligned.  What the…?

29HRD xformer2Yes, the feet and bottom of the frame is aligned.

30HRD xformer3But the top of the lamination stack is definitely displaced on the top.

31HRD xformer4Here, the laminations are parallel, but the straight edge shows that the old transformer is definitely parallelogrammed.

32HRD Broken Glass1A phone call to the owner reveals that this amp was in a serious car wreck about five years ago.

33HRD Broken Glass2That wreck explains why the bottom of this amp is filled with broken safety glass.  The force of the car wreck deformed the output transformer.  I’m guessing that as the deformed transformer heated up, the internal insulation broke down somewhere because the windings were stretched by the deformed transformer.

34HRD new xformer1Let’s bolt down the new transformer.  Here, the leads are fished through the grommet in the chassis.

35HRD new xformer2A replacement TieWrap is installed in place of the old one.  The small transformer is the power supply choke.

36HRD new xformer3More TieWraps are applied to dress the leads in a manner similar to the original.

37HRD cleanup panelI’m pretty confident that the unit will work fine now!  Let’s put everything together, including all those knobs!

38HRD input jacks2Here are the new jacks.

39HRD new finalsThe new output transformer deserves a new set of tubes.

40HRD new preampThese preamp tubes were ordered at the same time.

41HRD biasA one ohm resistor in series with the output plate circuit allows us to directly read the idle current of the output tubes.  60mV corresponds to 60mA of bias current, exactly what Fender specifies.

42HRD lower temp1Another temperature check is performed after everything warms up.

43HRD lower temp2This little thermometer came from Harbor Freight.  It works surprisingly well for a $20 infrared thermometer.

44HRD final final testWe are restarting the four hour test from the start.

45HRD happy ampIf you look closely, you can see a blue beam of electrons flying into the tube envelope through a small aperture in the plate.  These bottles are happy!

46HRD back homeThis road warrior has a new cover!

Listen to this amp in action at http://billybourbonmusic.com/ and support this artist!

Thanks for reading all the way to the end!

CONTACT – David Latchaw EE
281-636-8626

 

Digitech GSP1101 Effects Processor Repair

A frantic spouse called to explain that she was vacuuming and hit this ‘thing’ and broke this little piece off it.  Could I fix it before her husband found out?  The Unbrokenstring Crew to the rescue again!

01GSP brokenThe gain knob on this unit is a rotary encoder.  This component is available from several vendors.

02GSP what to doShe kept the knob, which is GREAT news, because although the rotary encoder is available, the knob is not.

03GSP salvage knobThe remains of the shaft of the rotary encoder was removed from the knob.  So far, so good.

04GSP opensesameLet’s get to work replacing the broken rotary encoder.

05GSP knobs offAs is the usual case, all the knobs come off first.

06GSP board looseThe circuit board lifts away easily.

07GSP spacer1These cool little plastic spacers set the geometry of the rest of the buttons and controls.

08GSP spacer2We will put this piece away somewhere safe while work elsewhere continues.

09GSP remove oldTo minimize the stress on the circuit board while removing the old component, the body of the broken rotary encoder is cut away from the component leads at an angle perpendicular to the circuit board.

10GSP part goneWith the component cut away from the circuit board, de-soldering the legs becomes trivial.

11GSP clear backThe component legs are gone.  This is a high-quality circuit board, double-sided copper and plated-thru holes.

12GSP clear frontBoth sides of the circuit board are cleaned up.

13GSP new partHere is the new part, ready to be soldered onto the circuit board.

14GSP reassemble1We are ready for reassembly.  That plastic spacer is re-installed as it was before.

15GSP reassemble2The cable carries all the signals back and forth to the front panel.  I like this bit of orgami.

16GSP reassemble3The circuit board is held in place by the bodies of the controls, which are in turn bolted to the front panel.

17GSP knobs onEverything is back together, ready for testing.

18GSP power onThis looks good!  While we were at it, we will do a factory reset.

19GSP final testNow, everything is as it once was.  And the husband was scolded for leaving his toys on the floor, where she could hit them with the vacuum.  Maybe I could sell him a rack case?

Thanks for reading all the way through!

CONTACT – David Latchaw EE
281-636-8626